Market Notices

123406POWER SYSTEM EVENTS17/01/2025 02:46:41 PM

Update Non-credible contingency event - NSW region - 17/01/2025

AEMO ELECTRICITY MARKET NOTICE.

Update Non-credible contingency event - NSW region - 17/01/2025

Refer AEMO Electricity Market Notice 123404

At 0825 hrs the Buronga 330 kV B Bus tripped.
AEMO did not instruct load shedding.

AEMO has not been advised of any disconnection of bulk electrical load.

The cause of this non credible contingency event is not known at this stage.

Manager NEM Real Time Operations
     
123405SETTLEMENTS RESIDUE17/01/2025 01:10:24 PM

[EventId:202501171310_NRM_NSW1_VIC1_started] NEGRES CONSTRAINT NRM_NSW1_VIC1 started operating from 17 January 2025 13:10

AEMO ELECTRICITY MARKET NOTICE

Issued by Australian Energy Market Operator Ltd at 1310 hrs on 17 January 2025

ACTUAL NEGATIVE SETTLEMENT RESIDUES - NSW to VIC - 17 January 2025.

Electricity Market outcomes have resulted in the accumulation of negative settlement residues that have exceeded the allowable negative residue threshold for the NSW to VIC directional interconnector.

The negative residue constraint set NRM_NSW1_VIC1 commenced operating from 1310 hrs on 17 January 2025.

This constraint set contains an equation with the following interconnectors on the LHS:
VIC1-NSW1

The RHS of the constraint equation may be adjusted to manage residues.


This is an AEMO autogenerated Market Notice.
     
123404POWER SYSTEM EVENTS17/01/2025 10:11:09 AM

Non-credible contingency event - NSW region - 17/01/2025

AEMO ELECTRICITY MARKET NOTICE.

Non-credible contingency event - NSW region - 17/01/2025

At 0825 hrs the Buronga 330 kV B Bus tripped.

AEMO did not instruct load shedding.

AEMO has not been advised of any disconnection of bulk electrical load.

The cause of this non credible contingency event has been identified and AEMO is satisfied that another occurrence of this event is unlikely under the current circumstances.

The cause of this non credible contingency event is not known at this stage.


Manager NEM Real Time Operations
     
123401RECLASSIFY CONTINGENCY16/01/2025 11:03:58 PM

Cancellation of a Non-Credible Contingency Event: Ross - Tully South - Woree No.8905 275 kV line line and Cardwell - Tully No.7389 132kV line line in QLD1 due to Lightning.

AEMO ELECTRICITY MARKET NOTICE

Cancellation of reclassification of a Non-Credible Contingency Event as a Credible Contingency Event due to Lightning. AEMO considers the simultaneous trip of the following circuits is no longer reasonably possible. There is no longer any lightning activity in the vicinity of the following lines. Accordingly its classification has reverted to a non-credible contingency event.

Region: QLD1

Lines: Ross - Tully South - Woree No.8905 275 kV line and Cardwell - Tully No.7389 132kV line

Cancellation time: 16/01/2025 23:03

Constraint set(s) revoked:
NONE

Refer AEMO Electricity Market Notice 123395

Auto-generated on behalf of Manager NEM Real Time Operations
     
123399RECLASSIFY CONTINGENCY16/01/2025 09:33:56 PM

Cancellation of a Non-Credible Contingency Event: Guybal Munjan - Chalumbin 857 275kV line line and Guybal Munjan - Chalumbin 858 275kV line line in QLD1 due to Lightning.

AEMO ELECTRICITY MARKET NOTICE

Cancellation of reclassification of a Non-Credible Contingency Event as a Credible Contingency Event due to Lightning. AEMO considers the simultaneous trip of the following circuits is no longer reasonably possible. There is no longer any lightning activity in the vicinity of the following lines. Accordingly its classification has reverted to a non-credible contingency event.

Region: QLD1

Lines: Guybal Munjan - Chalumbin 857 275kV line and Guybal Munjan - Chalumbin 858 275kV line

Cancellation time: 16/01/2025 21:33

Constraint set(s) revoked:
Q-RSCH_N-2 Constraint set contains the following interconnector(s) on the left hand side:
NONE


Refer AEMO Electricity Market Notice 123394

Auto-generated on behalf of Manager NEM Real Time Operations
     
123398RECLASSIFY CONTINGENCY16/01/2025 09:18:55 PM

Cancellation of a Non-Credible Contingency Event: Tumoulin - Woree No.877 275 kV line and Chalumbin - Turkinje No.7166 132 kV line in QLD1 due to Lightning.

AEMO ELECTRICITY MARKET NOTICE

Cancellation of reclassification of a Non-Credible Contingency Event as a Credible Contingency Event due to Lightning. AEMO considers the simultaneous trip of the following circuits is no longer reasonably possible. There is no longer any lightning activity in the vicinity of the following lines. Accordingly its classification has reverted to a non-credible contingency event.

Region: QLD1

Lines: Tumoulin - Woree No.877 275 kV and Chalumbin - Turkinje No.7166 132 kV

Cancellation time: 16/01/2025 21:18

Constraint set(s) revoked:
NONE

Refer AEMO Electricity Market Notice 123396

Auto-generated on behalf of Manager NEM Real Time Operations
     
123397RECLASSIFY CONTINGENCY16/01/2025 09:03:55 PM

Cancellation of a Non-Credible Contingency Event: Chalumbin - Turkinje No.7165 132 kV line and Chalumbin - Turkinje No.7166 132 kV line in QLD1 due to Lightning.

AEMO ELECTRICITY MARKET NOTICE

Cancellation of reclassification of a Non-Credible Contingency Event as a Credible Contingency Event due to Lightning. AEMO considers the simultaneous trip of the following circuits is no longer reasonably possible. There is no longer any lightning activity in the vicinity of the following lines. Accordingly its classification has reverted to a non-credible contingency event.

Region: QLD1

Lines: Chalumbin - Turkinje No.7165 132 kV and Chalumbin - Turkinje No.7166 132 kV

Cancellation time: 16/01/2025 21:03

Constraint set(s) revoked:
NONE

Refer AEMO Electricity Market Notice 123393

Auto-generated on behalf of Manager NEM Real Time Operations
     
123396RECLASSIFY CONTINGENCY16/01/2025 08:17:35 PM

Reclassification of a Non-Credible Contingency Event: Tumoulin - Woree No.877 275 kV line and Chalumbin - Turkinje No.7166 132 kV line in QLD1 due to Lightning.

AEMO ELECTRICITY MARKET NOTICE

Reclassification of a Non-Credible Contingency Event as a Credible Contingency Event due to Lightning. AEMO considers the simultaneous trip of the following circuits to now be more likely and reasonably possible. Accordingly AEMO has reclassified it as a credible contingency event.

Region: QLD1

Lines: Tumoulin - Woree No.877 275 kV and Chalumbin - Turkinje No.7166 132 kV

Duration: 16/01/2025 20:17 until further notice

Constraint set(s) invoked:
NONE

Auto-generated on behalf of Manager NEM Real Time Operations
     
123395RECLASSIFY CONTINGENCY16/01/2025 08:02:22 PM

Reclassification of a Non-Credible Contingency Event: Ross - Tully South - Woree No.8905 275 kV line line and Cardwell - Tully No.7389 132kV line line in QLD1 due to Lightning.

AEMO ELECTRICITY MARKET NOTICE

Reclassification of a Non-Credible Contingency Event as a Credible Contingency Event due to Lightning. AEMO considers the simultaneous trip of the following circuits to now be more likely and reasonably possible. Accordingly AEMO has reclassified it as a credible contingency event.

Region: QLD1

Lines: Ross - Tully South - Woree No.8905 275 kV line and Cardwell - Tully No.7389 132kV line

Duration: 16/01/2025 20:02 until further notice

Constraint set(s) invoked:
NONE

Auto-generated on behalf of Manager NEM Real Time Operations
     
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