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Correction - Non-credible contingency event - QLD region - 27/07/2024
Correction to Market Notice 117486
Non-credible contingency event - QLD region - 27/07/2024
At 0951 hrs the H38 Goodna No. 2 275kV Bus and the H38 Goodna No. 1 275/132kV transformer tripped.
AEMO did not instruct load shedding.
AEMO has not been advised of any disconnection of bulk electrical load.
The cause of this non credible contingency event is not known at this stage.
Manager NEM Real Time Operations
Non-credible contingency event - QLD region - 27/07/2024
Non-credible contingency event - QLD region - 27/07/2024
At 0951 hrs the H3 Goodna No. 2 275kV Bus and the H3 Goodna No. 1 275/132kV transformer tripped.
AEMO did not instruct load shedding.
AEMO has not been advised of any disconnection of bulk electrical load.
The cause of this non credible contingency event is not known at this stage.
Manager NEM Real Time Operations
Cancellation of Actual (LOR1) condition in the NSW region - 03/07/2024
Cancellation of Actual (LOR1) condition in the NSW region - 03/07/2024
The Actual LOR1 Condition in the NSW Region advised in AEMO Electricity Market Notice No.117284 is cancelled at 2010 hrs 03/07/2024.
Manager NEM Real Time Operations
Actual Lack Of Reserve Level 1 (LOR1) in the NSW region - 03/07/2024
Actual Lack Of Reserve Level 1 (LOR1) in the NSW region - 03/07/2024
An Actual LOR1 condition has been declared under clause 4.8.4(b) of the National Electricity Rules for the NSW region from 1730 hrs.
The Actual LOR1 condition is forecast to exist until 1930 hrs
The capacity reserve requirement is 1400 MW
The minimum capacity reserve available is 766 MW
Manager NEM Real Time Operations
Non-credible contingency event - NSW region - 27/06/2024
Non-credible contingency event - NSW region - 27/06/2024
At 0845 hrs the Sydney West No.1 330 kV SVC tripped during switching for planned outage of Sydney West No.4 330/132 kV transformer.
AEMO did not instruct load shedding.
AEMO has not been advised of any disconnection of bulk electrical load.
The cause of this non credible contingency event is not known at this stage.
Manager NEM Real Time Operations
Non-credible contingency event - NSW region - 25/06/2024
Non-credible contingency event - NSW region - 25/06/2024
At 0901 hrs the Sydney West No.1 330 kV SVC tripped during switching for planned outage of Sydney West No.4 330/132 kV transformer.
AEMO did not instruct load shedding.
AEMO has not been advised of any disconnection of bulk electrical load.
The cause of this non credible contingency event has been identified and AEMO is satisfied that another occurrence of this event is unlikely under the current circumstances.
AEMO will not reclassify this event as a credible contingency event.
Manager NEM Real Time Operations
Cancellation of Actual (LOR1) condition in the NSW region - 20/06/2024
Cancellation of Actual (LOR1) condition in the NSW region - 20/06/2024
The Actual LOR1 Condition in the NSW Region advised in AEMO Electricity Market Notice No.117086 is cancelled at 1930hrs 20/06/2024.
Manager NEM Real Time Operations
Actual Lack Of Reserve Level 1 (LOR1) in the NSW region - 20/06/2024
Actual Lack Of Reserve Level 1 (LOR1) in the NSW region - 20/06/2024
An Actual LOR1 condition has been declared under clause 4.8.4(b) of the National Electricity Rules for the NSW region from 1800 hrs.
The Actual LOR1 condition is forecast to exist until 1900 hrs
The capacity reserve requirement is 1726 MW
The minimum capacity reserve available is 1695 MW
Manager NEM Real Time Operations
Non-credible contingency event - VIC region - 18/06/2024
Non-credible contingency event - VIC region - 18/06/2024
At 0839 hrs the Glenrowan No1 66kV Bus tripped.
AEMO did not instruct load shedding.
AEMO has not been advised of any disconnection of bulk electrical load.
The cause of this non credible contingency event is not known at this stage.
Manager NEM Real Time Operations