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Cancellation - Non-credible contingency event - QLD region - 27/01/2024
Cancellation - Non-credible contingency event - QLD region - 27/01/2024
Refer AEMO Electricity Market Notice 113825
At 0138 hrs the Gin Gin (H6) No.2 275 kV Busbar tripped.
AEMO has received further information and now determines this was not a non-credible contingency event.
Manager NEM Real Time Operations
PDPASA - Update of the Forecast Lack Of Reserve Level 2 (LOR2) in the QLD Region on 27/01/2024
The Forecast LOR2 condition in the QLD region advised in AEMO Electricity Market Notice No. 113840 has been updated at 1400 hrs to the following:
[From 1900 hrs 27/01/2024 to 1930 hrs 27/01/2024.
The forecast capacity reserve requirement is 520 MW.
The minimum capacity reserve available is 514 MW.
AEMO is seeking a market response.
Manager NEM Real Time Operations
STPASA - Update of the Forecast Lack Of Reserve Level 2 (LOR2) in the QLD Region on 30/01/2024
The Forecast LOR2 condition in the QLD region advised in AEMO Electricity Market Notice No. 113829 has been updated at 1400 hrs 27/01/24 to the following:
From 0800 hrs 30/01/2024 to 1300 hrs 30/01/2024.
The forecast capacity reserve requirement is 883 MW.
The minimum capacity reserve available is 505 MW.
AEMO is seeking a market response.
AEMO has not yet estimated the latest time at which it would need to intervene through an AEMO intervention event.
AEMO Operations
PDPASA - Update of the Forecast Lack Of Reserve Level 2 (LOR2) in the QLD Region on 27/01/2024
The Forecast LOR2 condition in the QLD region advised in AEMO Electricity Market Notice No. 113827 has been updated at 1130 hrs to the following:
From 1800 hrs 27/01/2024 to 2030 hrs 27/01/2024.
The forecast capacity reserve requirement is 520 MW.
The minimum capacity reserve available is 315 MW.
AEMO is seeking a market response.
AEMO estimates the latest time it would need to intervene through an AEMO intervention event is 1230 hrs on 27/01/2024.
Manager NEM Real Time Operations
STPASA - Cancellation of the Forecast Lack Of Reserve Level 2 (LOR2) in the QLD Region on 28/01/2024
The Forecast LOR2 condition in the QLD region advised in AEMO Electricity Market Notice No. 113828 is cancelled at 1100 hrs 27/01/2024.
Manager NEM Real Time Operations
STPASA - Forecast Lack Of Reserve Level 2 (LOR2) in the QLD Region on 30/01/2024
AEMO declares a Forecast LOR2 condition under clause 4.8.4(b) of the National Electricity Rules for the QLD region for the following period:
From 0830 hrs 30/01/2024 to 0900 hrs 30/01/2024.
The forecast capacity reserve requirement is 774 MW.
The minimum capacity reserve available is 709 MW.
AEMO is seeking a market response.
AEMO has not yet estimated the latest time it would need to intervene through an AEMO intervention event.
Manager NEM Real Time Operations
STPASA - Forecast Lack Of Reserve Level 2 (LOR2) in the QLD Region on 28/01/2024
AEMO declares a Forecast LOR2 condition under clause 4.8.4(b) of the National Electricity Rules for the QLD region for the following period:
[1.] From 1300 hrs 28/01/2024 to 1400 hrs 28/01/2024.
The forecast capacity reserve requirement is 651 MW.
The minimum capacity reserve available is 564 MW.
AEMO is seeking a market response.
AEMO has not yet estimated the latest time it would need to intervene through an AEMO intervention event.
Manager NEM Real Time Operations
PDPASA - Update of the Forecast Lack Of Reserve Level 2 (LOR2) in the QLD Region on 27/01/2024
The Forecast LOR2 condition in the QLD region advised in AEMO Electricity Market Notice No. 113824 has been updated at 0745 hrs to the following:
From 1700 hrs 27/01/2024 to 2200 hrs 27/01/2024.
The forecast capacity reserve requirement is 541 MW.
The minimum capacity reserve available is 131 MW.
AEMO is seeking a market response.
AEMO has not yet estimated the latest time at which it would need to intervene through an AEMO intervention event.
Manager NEM Real Time Operations
Non-credible contingency event - QLD region - 27/01/2024
Non-credible contingency event - QLD region - 27/01/2024
At 0138 hrs the Gin Gin (H6) No.2 275 kV Busbar tripped.
AEMO did not instruct load shedding.
AEMO has not been advised of any disconnection of bulk electrical load.
The cause of this non credible contingency event is not known at this stage.
Manager NEM Real Time Operations