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Non-credible contingency event - QLD region - 21/10/2023
Non-credible contingency event - QLD region - 21/10/2023
At 0133 hrs the Ross No 2 275kV Bus tripped.
AEMO did not instruct load shedding.
AEMO has not been advised of any disconnection of bulk electrical load.
The cause of this non credible contingency event is not known at this stage.
Manager NEM Real Time Operations
Non-credible contingency event - VIC region - 19/10/2023
Non-credible contingency event - VIC region - 19/10/2023
At 1437 hrs the Moorabool No.2 500kV bus tripped
AEMO did not instruct load shedding.
AEMO has not been advised of any disconnection of bulk electrical load.
The cause of this non credible contingency event has been identified and AEMO is satisfied that another occurrence of this event is unlikely under the current circumstances.
AEMO will not reclassify this event as a credible contingency event.
Manager NEM Real Time Operations
Update - Non-credible contingency event - SA region - 17/10/2023
Update - Non-credible contingency event - SA region - 17/10/2023
Refer AEMO Electricity Market Notice 110289
At 0845 hrs the Penola_W Kincraig 132kV line was returned to service.
The cause of this non-credible contingency event has been identified and AEMO is satisfied that another occurrence of this event is unlikely under the current circumstances.
AEMO will not reclassify this event as a credible contingency event.
Manager NEM Real Time Operations
Non-credible contingency event - SA region - 17/10/2023
Non-credible contingency event - SA region - 17/10/2023
At 0711 hrs the Penola_W Kincraig 132kV line offloaded at one end only, during switching for planned outage of Kincraig No.1 132/33/11kV transformer.
AEMO did not instruct load shedding.
AEMO has not been advised of any disconnection of bulk electrical load.
The cause of this non credible contingency event is not known at this stage.
Manager NEM Real Time Operations
Non-credible contingency event - SA region - 13/10/2023
Non-credible contingency event - SA region - 13/10/2023
At 1402 hrs, the Para 6543 275kV CB tripped offloading the Para No.2 275/66kV transformer at one end only.
AEMO did not instruct load shedding.
AEMO has not been advised of any disconnection of bulk electrical load.
The cause of this non credible contingency event is not known at this stage.
Manager NEM Real Time Operations
Update - Non-credible contingency event - SA region - 12/10/2023
Update - Non-credible contingency event - SA region - 12/10/2023
Refer AEMO Electricity Market Notice 110232
At 1609 hrs the South East Nos 1 and 2 SVCs were returned to service.
The cause of this non-credible contingency event has been identified and AEMO is satisfied that another occurrence of this event is unlikely under the current circumstances.
AEMO will not reclassify this event as a credible contingency event.
Manager NEM Real Time Operations
Non-credible contingency event - SA region - 12/10/2023
Non-credible contingency event - SA region - 12/10/2023
At 1524 hrs the South East No1 SVC and the South East No2 SVC tripped.
The cause of this non credible contingency event is not known at this stage.
Manager NEM Real Time Operations
Update - Non-credible contingency event - SA region - 14/09/2023
Update - Non-credible contingency event - SA region - 14/09/2023
Refer AEMO Electricity Market Notice 109807
At 1920 hrs the South East-Mayura-Snuggery 132kV LINE was returned to service.
The cause of this non-credible contingency event has been identified and AEMO is satisfied that another occurrence of this event is unlikely under the current circumstances.
AEMO will not reclassify this event as a credible contingency event.
Manager NEM Real Time Operations
Non-credible contingency event - SA region - 14/09/2023
Non-credible contingency event - SA region - 14/09/2023
At 1450 hrs the Snuggery CBs 6131 and 6028 opened automatically, offloading the South East-Mayura-Snuggery 132kV LINE at the Snuggery end only.
AEMO did not instruct load shedding.
AEMO has not been advised of any disconnection of bulk electrical load.
The cause of this non credible contingency event is not known at this stage.
Manager NEM Real Time Operations